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| NTSB Identification: DEN99LA174. The docket is stored in the (offline) NTSB Imaging System. |
| Accident occurred Sunday, September 05, 1999 at SANTA FE, NM |
| Aircraft: Cessna P210N, registration: N999KM |
| Injuries: 2 Uninjured |
| Event: 20001212X19751 Status: Final Report Approved On Thursday, November 02, 2000 |
| NTSB Preliminary Narrative (6120.19A) |
| On September 5, 1999, approximately 1010 mountain daylight time, a Cessna P210N, N999KM, was substantially damaged when it collided with |
| terrain during a forced landing 10 miles west of Santa Fe, New Mexico. The private pilot, the sole occupant aboard, was not injured. Visual |
| meteorological conditions prevailed, and an IFR flight plan had been filed for the business flight being conducted under Title 14 CFR Part 91. The |
| flight originated at Santa Fe approximately 1000. |
| The airplane was equipped with a Rolls Royce (Allison) 250-B17F turbine engine. The pilot said that in preparation for his return flight to San |
| Jose, California, he had all the fuel tanks (wings, tips, fuselage) topped off with Jet-A fuel (about 147 gallons) and Prist, a fuel additive. He said |
| that on his first attempt to start the engine, N1 reached only about 30% with no temperature rise, so he stopped the start sequence. After |
| waiting five minutes, a second start attempt was successful. Peak turbine outlet temperature (TOT) was 707 degrees C. Taxi, runup, and |
| takeoff were said to be normal. |
| The pilot said about 10 minutes after departure, as the airplane was climbing through 12,000 feet msl (mean sea level), "the engine stopped, the |
| generator light came on, and the torque needle went to zero." An inflight restart was attempted but was not successful. The pilot made a |
| forced landing on Highway 16. Oncoming traffic forced the pilot to depart the side of the road, shearing off the nose wheel at the fork. |
| Damage was originally assessed to be minor and the mishap was classified as an incident. Subsequent examination disclosed negative buckling |
| of the spar web and cap caused by the wings flexing during the off roadway excursion. |
| According to Allison, a Federal Aviation Administration inspector "motored" the engine at least 3 times without verifying the amount of fuel in the |
| lines and filters. The engine was shipped to National Airmotive for testing. On October 5 and 6, the fuel control was tested. After being |
| reattached, the engine was started and stabilized at idle. Shortly thereafter, TOT began to rise and oil pressure dropped slightly. The engine |
| was shut down. Two other engine starts were aborted due to high TOT. The next two engine starts were normal but the gearbox pressure |
| was high. The engine was again shut down. On October 7, two engine starts were made. The first ended in a premature shutdown when |
| "test stand hysteresis" caused the test cell throttle linkage to move to the OFF position. The second start was successful and performance |
| calibration was completed. |
| NTSB Final Narrative (6120.4) |
| The airplane was equipped with a Rolls Royce (Allison) 250-B17F turbine engine. All the fuel tanks (wings, tips, fuselage) were topped off with |
| Jet-A fuel (about 147 gallons) and Prist, a fuel additive. During the first attempt to start the engine, N1 reached about 30% with no temperature |
| rise, so the pilot stopped the start sequence. After waiting about five minutes, a second start attempt was successful. Peak turbine outlet |
| temperature (TOT) was 707 degrees C. Taxi, runup, and takeoff were normal. About 10 minutes after departure, as the airplane was climbing |
| through 12,000 feet msl, 'the engine stopped, the generator light came on, and the torque needle went to zero.' An inflight restart was attempted |
| but was not successful. The pilot made a forced landing on Highway 16. Oncoming traffic forced the pilot to depart the side of the road |
| shearing off the nose wheel at the fork. The wings flexed during the off roadway excursion, causing the spar web and cap to buckle |
| downward. The engine was later functionally tested successfully. |
| NTSB Probable Cause Narrative |
| A non-mechanical total loss of engine power for reasons undetermined. Factors were maneuvering to avoid oncoming vehicles, and the rough |
| and uneven terrain. |
| Occurrences and Sequence of Events |
| Occurrence: 1, LOSS OF ENGINE POWER(TOTAL) - NONMECHANICAL |
| Phase of Operation: CLIMB - TO CRUISE |
| Sequence of Events for Occurrence Number: 1 |
| 1 ( Cause ) REASON FOR OCCURRENCE UNDETERMINED / / |
| Occurrence: 2, FORCED LANDING |
| Phase of Operation: DESCENT - EMERGENCY |
| Occurrence: 3, NOSE GEAR COLLAPSED |
| Phase of Operation: LANDING - ROLL |
| Sequence of Events for Occurrence Number: 3 |
| 1 ( Factor ) MANEUVER TO AVOID OBSTRUCTIONS / INTENTIONAL / PILOT IN COMMAND |
| 2 ( Factor ) OBJECT / VEHICLE / (0) |
| 3 ( Factor ) TERRAIN CONDITIONS / ROUGH/UNEVEN / (0) |
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